Fitting The Elevators to the Horizontal Stabilizer

The empennage kit is wrapping up, and almost complete at this point.  All the major assembly is done, and now its just fitting the parts together and lining up the hinges to drill the elevator horns.  The first thing to do is make sure the eye bolts on the elevators … Continue reading

Closing and Finishing the Horizontal Stabilizer

Since I have had my horizontal stabilizer inspected and approved, I am ready to close it up and finish it! I started tonights session by re-clecoing the front spar onto the horizontal stabilizer.  I had removed it so the inspector could get a good look inside and check my work. … Continue reading

Finishing the Horizontal Stabilizer Skin

I was able to finish up riveting on the skins of both sides of the horizontal stabilizer.  I had only planned to rivet on the right side skin to HS-702 front spar and HS-708 rib, but that only took about a half hour to complete.  So, I decided I should … Continue reading

Riveting the right horizontal stabilizer

Tonight I spent about 1.5 hours on riveting the right horizontal stabilizer.  I am very close to getting these skins riveted on, and almost to the point of attaching the rear spar.  I have decided to wait on attaching the rear spar until I can get an EAA Tech Counselor … Continue reading

Riveting the Horizontal Stabilizer

I spent about 3.5 hours on riveting the horizontal stabilizer, and ended up getting the left side completed, and ready for the rear spar.  I also got a start on the right side and have it ready for final riveting. First off I riveted the HS-706 to the front spar … Continue reading

Riveting the Left Horizontal Stabilizer

Tonight started off by riveting the HS-00005 and HS-00006 ribs to the HS-702 front spar.  I was able to use my squeezer to set these rivets, but only just barely! I had to do some finagling around the front spar support bars, especially the larger HS-714 to get the squeezer … Continue reading

Dimpling the Left Horizontal Stabilizer

After riveting the front spar, I was still wanting something to do, but nothing very involved.  I realized I hadn’t dimpled my skins yet, since I was waiting to do that until after the primer had cured.   Since the next step in the plans call for me to rivet on a few ribs to the left skin, I figured this was just a good a time as any to start!

I used the DRDT-2 dimpling tool to dimple all my skins.  I used a piece of scrap aluminum to set the dimple dies and the compression on the dimpler to form a perfect skin dimple.  A lot of folks don’t do this step since, and just go right to dimpling.  There’s nothing wrong with doing that, but there is an issue of under-dimpling which causes the skin to look like it has a “dished in” surface around the dimple.  You end up with this weird wavy looking skin surface.  Again, theres probably nothing wrong with have an under dimpled skin, so long as the part fit together snug, but I am wanting to build a quality airplane that looks excellent, so I take the extra time to set these things.  After a few test dimples in my test coupons of aluminum, I started on my left horizontal stabilizer.

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The DRDT-2 makes this work a breeze!  I still need to get some carpet or moving blankets so that I don’t have to worry about my work surface scratching my skins.  Right now I am using the plans manual under the skin to keep it off the rough work bench.  It works, but not ideal.  It takes a good bit of pressure to get a solid, clean dimple.  I am also using spring-back dimple dies from Cleaveland tool and they need a good bit of pressure to form a good dimple. I spent about an hour going around the skin bottom.  Then I marked off the top side of the skin using masking tape.  There are a few rivet holes that will be used later on to install the tail fairing, and we use nutplates for that.  So, Van’s has you not dimple a few holes in the top skin.  I covered them with masking tape so I wouldn’t accidently dimple them.

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This process went pretty quickly because of the dimpler.  I did have a few tricky holes towards the leading edge of the skin (where it curves/wraps around).  I had to take the skin off the table, and hold it with the opposite hanging down in front of the dimpler so I could reach them.  All in all, I think the dimples came out great.  I test fit them with a spare AN426AD-3-4 rivet, and the rivet fits in perfectly and there is no wavy-ness or under dimpled holes.

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Since I won’t be working on the right skin for a few more work sessions, I figured it was time to stop.  It was also close to 1:15 AM, and I was a little tired by this point.  I’ve always heard its good to stop before you get tired, because you will make a mistake.

Heres all the photos from tonights work session: https://goo.gl/photos/8H9dqyZWPKZR22A77

Hours Worked: 1.0

Dimpling the Right Horizontal Stabilizer

I didn’t have much time tonight, I was working on my parade car most of the day. But, I did find a little over an hour to get some work done on the airplane.  My beam torque wrench was delivered today, so I also torqued the bolts that hold the HS-411 hinge bracket to the rear spar.  Referring to the chart in the Van’s manual, I am supposed to torque the AN3 bolts down to 20-25 inch pounds, adding in the torque required to turn the nylon lock nuts.  My beam wrench was showing 5-8 inch pounds required to turn the nylon nut on the AN3 bolt, so I figured I would torque the bolts down to a total of 28-30 inch pounds.  After torquing the nuts down, I marked them with an “X” using a sharpie.  I will apply some torque seal once it gets here. This way I know which bolts have been torqued.

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Having completed that, I figured I should go ahead and dimple the right horizontal stabilizer skin, since I had a little bit of time left for the night. I used my DRDT-2 dimpler to do the work, and it went smoothly. I already had the dimpler set up from last nights work, so I just popped in the sets, and went at it.  I also remembered to mask off the holes in the skin that do not need dimpling, since they will be getting nut plates. The skin turned out well.

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And for some reason, my camera decided to make a little video.  I must have flipped a switch somewhere, so for fun, here is the video my camera made for us:

I spent a few minutes tinkering around with the pressure settings on my rivet gun.  I will be riveting the ribs to the skins in a few sessions, so I want to make sure I have everything set right.  I think I might spend some more time on the practice kits doing flush rivets over again.  This will give me some more practice, as well as let me fine tune my rivet gun for the -3 flush rivets.

Here is a full photo album of tonights work: https://goo.gl/photos/upb27wsi3J5HnDuu5

Hours Worked: 1.25

Front Spar Riveting

My torque wrench hasn’t shown up yet, so I wasn’t able to finish up the last steps on the rear spar.  I decided to continue on to the front spar and return to the rear once I get my wrench and can torque those 4 last bolts to the proper specs.  The next step in the plans is to rivet the front spar assembly.

I started out by clecoing HS-710, HS-714, and HS-00001 onto the HS-702 front spar, so I could make sure everything lines up correctly before riveting. img_0735

The plans call for a AN470AD4-7 rivet where the HS-710 and HS-714 go together with the HS-702 front spar and the HS-00001 doubler plate.  There are also a few location where you do not want to rivet, because the HS-000005 and HS-00006 ribs will attach later, as well as the holes that will be drilled later when the tail is attached to the fuselage.   To keep myself from sticking a rivet in those holes, I covered them with masking tape. The only photo I have of my masking tape is from AFTER driving the rivet.

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I used my squeezer to drive all these rivets which made it super easy to get them correct.  Once I drove all the longer -7 rivets, I moved on to drive the shorter AN470AD4-5 rivets where the HS-00001 doubler plate attaches to the HS-702 spar.  These are shorter because they don’t have to go through the thick spar reinforcement bars.  You can see the two rows of these rivets in the middle of the spar in the photo above.

The next step was to rivet the 4 flush head rivets into the HS-702 to HS-710 / HS-714 reinforcement bars.  I had previously countersunk the bars, and dimpled the spar, so these 4 were easy to set with the squeezer.

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After squeezing those last 4 flush head rivets, my front spar assembly was completed.  I am pretty happy with the way it came out. I didn’t have to drill out any rivets, and I made sure they were all set correctly by measuring each and every one with the rivet gauge.  This is how it looked once it was all done and completed.  I removed the masking tape since it’s not going to be needed anymore.

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Here is a link to all the photos I took for this work session: https://goo.gl/photos/Swd5BBf6HfW5jP2h9

Hours Worked: 2.5

Fixing the Bad Rivet in the Rear Spar

After reading some of the replies on what I should do about my messed up rivet, I decided to drill it out. I had some time to work on this before we head out to my parents house for thanksgiving, so I figured I would try to drill it out.

First I used a my noxon punch to dimple a point in the head of the rivet. The little center dimple from the factory was barely visible, so I used it to center my punch. Then I took a fresh #40 bit and slathered it in boelube and chucked it up. I put it in the center punched dimple, and turned it by hand a few times to get the bit started. Then I slowly drilled the head down deep enough I could break the head off with the butt end of an old drill bit.

Then I got a bit creative…. I didn’t have a receiving bar to drive the rivet into, so I ended up using a pair of vice grips. I stuck the jaws into a pair of leather gloves to keep from scratching the parts, and opened the jaws just enough so the rivet would fall into it. Then I used a punch and a small hammer to gently drive the old rivet out. My vise grips/glove worked pretty good as it received the rivet, and didn’t scratch my skins!

I checked the rivet and noticed that I had drilled perfectly center, and then checked the parts and the hole was undisturbed, so a regular rivet should work OK.

I stuck in a replacement normal rivet (AN470AD4-7) and squeezed it making sure I had my squeezer lined up and centered. It turned out great, and took about 30 minutes total time, since I was being cautious. I did end up scratching the nice paint (that I bought from Paint Booths) on my bracket, I dropped the stupid punch as I pulled it away and the tip dug into the paint a little. Doesn’t appear to be anything than just paint, so I will hit it with some rattle can primer to seal it up against corrosion, and let it ride. Here is the end result, with a fresh rivet:

I also learned that the washer should go on the nut side of my HS-411PP and that I should torque it to roughly 25 inch/lbs. I ended up buying this torque wrench so that I can read what the torque is from the nylon lock nut, and then add that to my final torque value: http://amzn.to/2gl2Axd

Once the wrench gets here, I will torque down the AN3 bolts and apply some torque seal (also on the way). Here is the photos from what little work I did today: https://goo.gl/photos/kxhRmW3LXQTkWas9A

Hours Worked: .5